914 DTM development and Hybrid 2316 testing!

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MASSIVE TYPE IV
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914 DTM development and Hybrid 2316 testing!

Post by MASSIVE TYPE IV »

19 Gallons of fuel, 24 full 2000-7500 RPM Dyno runs, Two FULL 12 hour days of trial, error, tuning and parts swapping- Its done!

Yesterday started out witha 140 HP first pull and disappointment- Today ended up with a whopping 40 HP tuned into the engine with no internal changes!!!!!

The DTM was really the easy part of this one! I knew from the minute it fired up and broke 200 degrees evenly on the quad CHT gauge that it was going to be a very easy task of perfecting the DTM for the 914. fact is we only had to make TWO small changes to the vanes to get the temps within 15 degrees of each other all around the engine! Plenum pressure differentials were less than 1PSI on both sides of the engine, and velcoity was within 3-4%! Pretty damn good for the first try with a slower than normal fan over drive (looking for power)

In cooling system runs we were seeing head temps with a 14 lb load at 4000 RPM of only 300 degrees! That was with a 180HP engine! The stock 100HP 2.0 runs FIFTY+ degrees hotter than that!!!!!!

As for the Hybrid engine and its power results- It kicked my ass. These heads, pistons, intakes and camshaft were all one off first time beasts. Due to this Brent and I fought for two full days with combinations of timing and jetting and even velocity stack and venturi sizes to find the perfect combo for the flattest torque curve, coolest temps and best EGT and BSFC numbers. Any time that we have a new combo with this many changes the dyno session is a huge learning curve when we are making the recipe's for all other "like" engines in the future that will follow in its foot steps- so what we do now is important for years to come, untio we supercede the combination.

This one was a pure b-itch! Lens heads are so efficient that they did not like typical timing settings (only 24 degrees Vs 28-30 for a typical 2.0 head) and they didn't want very much jetting at all either, but they did like a gross amount of airflow.

This being the first engine of a new series- it did not meet my expectations of 190 HP. There are many reasons for this, the biggest being my camshaft choice. The cam I chose was NOT split duration. Len and I both felt that a straight pattern cam would benefit these heads- But we were wrong and the EGT I was monitoring was indicative of this in every dyno run we made. This engine did make exceptional HP as it is set up with LESS compression than the older "Annihilator" engine (9.5 now Vs 10.2:1 before) and a flatter more stable torque curve. The efficiency of this new engine is MUCH higher and it is running a gob more efficiently.

Basically the old engine made 1HP more but 7 lb/ft less torque with 15% less gross torque across the board! Len and I designed these heads to have exceptional velocity and not alot of gross CFM. This helps with efficiency, and pulling out of turns and overall throttle response. While the Dyno shows equal peak power I felt the difference in the controls and I have a good hunch that this puppy will be MUCH faster in the car than the old engine was.

This engine was the first for many new developments, coatings and tolerances. Below I will go over a few of them and what we found.

*I tried a new rod bearing for this engine. It is a NASCAR bearing that I narrowed myself to fit the Buick rod journal. This bearing coupled with my ION Nitrided crank and Pc-2 coating on the bearing made for a super low friction arrangement. This bearing and set up was set up with .001 less running clearance than normal- to a totally dangerous level- But it works exceptionally, even after 12 - 8,000 RPM full pulls!

* This engine received Full DLC coatings on all load bearing surfaces. (pushrod tips, rocker shafts, dizzy drive pinion, wrist pins, etc) These coatings reduce friction by up to 75% and the oil temps were indicative of this! I have never seen oil temps this coo, in an engine of this tune! I plan on ripping this engine down after the race season and checking for wear differences with the DLC coatings. We set our valve/stem clearance with DLC coated valves to ONE HALF of one thousandth- A scary level without DLC, but totally acceptable with it so far! This means less crankcase pressure past the guides, less guide wear and better valve stem support for higher revs with less spring tension

* Our new super light valve train with 7mm stems and a few parts that Len and I dreamed up worked exceptionally! With the ceramic lifters(58 Gr), Titanium pushrods, lightened stock rockers (lightened 15 gr) with lightened 911 adjusters(lightened 2 gr) and lightweight retainers we were able to retain valve control at sub 8300 RPM levels! This was achieved with only 230 pounds of OPEN spring tesnion and 120 closed tension! This is unheard of but severely impacted by the cam lobe characteristics, and dampening of the oddball valve springs! We now have a fool proof, easy to use and very cheap 7mm arrangement for high revving Street and Race engines! Time will tell more about its strength.

* We tried something new with Nickies and skirt clearance. To keep crankcase pressure down at high RPM and reduce blowby we ran only .001 of skirt clearance, thats a full .001 LESS than normal with Nickies! The engine has hardly any blowby- even when intentionally overheated.

* I also tried a total seal rings with Nikisil- Another risky situation as the support rail for the gapless ring is a chrome ring. Total seal said it wouldn't work, but Charles and I thought it would. After 24 full dyno runs the cranking compression and leak down is unbelievable! It seems to be working as oil consumption is non existant, and crankcase pressure is as well. It is much lower than we have ever noted with the conventional JE ring pack that we use with the Nickies. Total seal rings typically have severe issues with break in with a cast iron cylinder- These broke in with the Nickies on the first power pull! Its too early to see exactly what the outcome will be, but after a few Autocrosses, and Driver's ed events I'll know! We may have made a big risk here with some beneficial results!

* I gathered even more Velocity stack data and venturi data and their impacts on powerband with different tuning characteristics....... This engine didn't want a super short stack, but rather a factory Weber stack- Totally odd!

* Gathered data for the DTM venturi ring, and proved that it makes the cooling fan noise significantly less than without it installed.

So........What would I change in the combo if I did it again??? Well definately the cam! I'd use the same master grind, but add atleast 5 degrees of split to the exhaust side of the profile and possibly grind it on a 104 lobe center for a faster opening event to take even more advantage of these awesome heads! I plan on ripping it down for an inspection over next winter and I'll make those changes and redyno to see the differences.

I would rip it apart now, but I need to get this engine fitted into the car to finish the development of the 914 DTM and I also have to go spank some ass at the Southeast Dyno day on March 5th.....

The DTM and its internals are perfect, we will fit the engine into my 914 tomorrow, cut out the templates, scan them into autocad and get the waterjet on the ball with making them.

After Dyno Day I should have sufficient in car test results to support my dyno data to prove the DTM owrks. I will then rip this version of the shroud off then 914, make a mold for it and be fitting the next version with an oil cooler provision ASAP..... If that one works well on the first try like this one I should have TWO perfected 914 systems with molds made by mid summer!

Sorry for the long post- but it's 4Am and the mad scientist isn't tired yet! I'll post pics and graphs to my R&D portion of the site tomorrow.
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Wally
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Post by Wally »

Due to the time difference, I am wide awake as well :lol: (but its an unfair comparison :wink: )

I love your R&D stuff Jake! Your comment and considerations are also very valuable, maybe even more.

What header/exhaust did you use? Could there be some 'bolt-on' gain left?
Why didn't you use the Kits system for induction? Testing/comparison reasons? It sure wouldn't be misplaced to use your EFI system on such an otherwise super high tech engine...

Thanks,
Walter
T4T: 2,4ltr Type 4 Turbo engine, 10.58 1/4 mi
www.apfelbeck.nl
"Mine isn't turbo'd to make a slow engine fast, but to make a fast engine insane" - Chip Birks
MASSIVE TYPE IV
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Post by MASSIVE TYPE IV »

Thanks Wally,
I have one of Chris' Tangerine Headers for my 914 with his phase 9 silencer. I did all testing with this system as it fits my car like a glove and has always performed so much better than the other 914 specific systems. I did test it with the Aero Turbine muffler and saw a very close comparison with it in place of the phase 9. I will try them both in the car and see which one works the best. What is so odd is that in the exhaust system testing the Aero Turbine sucked, on this engine it did not!

I did not use Kit Carlson for one main reason- Simplicity. This engine goes in and out of the car alot and I don't want wire harnasses and etc in the way.

Plus, when this engine is perfected it will pretty much be sold to a customer base that will use carbs with it- so the carb data and settings were important for me to make.
HAM Inc
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Post by HAM Inc »

WOW! 40HP from tuning alone! Let that be a lesson to everyone out there that the cheapest HP available is still dyno time with someone that knows what they're doing and has the patience to do it. It also underscores the importance of buying integrated engine kits, especially if dyno time is not an option.

I could never have done this kind of cylinderhead development without Jakes input. He was gracious enough to shoulder some of the responcibility for the straight pattern cam. The truth is after seeing the tremendous flow #'s out of the newly developed sq.port (it exceeded the 75-80% mark we shoot for) I convinced him it wouldn't be needed. I should have trusted Jake with this as he knows his ex. system better than I do.

We gained a boatload of new knowledge with this engine. We went WAY out on a limb with some of the ideas. Sometimes this bites you. With the uncharted territory on the lightwt. valve train and low (and I mean LOW) spring pressures if I'd been in the dyno room I would have closed my eyes when that baby hit 8,300RPM's.

These heads incorporated some very alternative ideas. High velocity and not to much concern for flow #'s. In that respect this is a very conservative package. We attacked valve-train stability problems at the source, valve weight, rather than just throwing stiffer springs at it. And trust me when I say we took this to the extreme. I have never set heads with springs this light. And when we were in the design stages the target RPM was 7200. If I'd known Jake was going to twist it that hard I wouldn't have gotten an hours sleep last night!

With this being the prototype I believe that with some more development we will make even bigger leaps in TypeIV possibilities that just a year ago were not even on paper.
Way to go Jake!
MASSIVE TYPE IV
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Post by MASSIVE TYPE IV »

Thanks Len!

Hey, the first time we rarely perfect anything, BUT we gain valuable info for the next try...

Next time I bet we'll see 10 more ponies from this baby atleast with just a cam change!
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Plastermaster
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Post by Plastermaster »

I see all this as very significant. It is one thing for the heads to like less timing advance, and less fuel. That is a sign of efficiency. When it surprises you with cam selection, when you already know the flow #s and the ratio, it shows the head work has really moved into uncharted territory as to how the heads are making power. It looks to me like you guys are really breaking ground. Or else you just didn't explain the rules clearly to these new heads. LOL

Ron
MASSIVE TYPE IV
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Post by MASSIVE TYPE IV »

True..
I think with a better cam the engine would like even less timing! Maybe as little as 20 degrees!
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Plastermaster
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Post by Plastermaster »

What is the primary advantage of the 7mm stems? Is it mostly the weight reduction, or more to do with less resistance to air flow?

Thanks

Ron
Racer Chris
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Post by Racer Chris »

Plastermaster wrote:What is the primary advantage of the 7mm stems? Is it mostly the weight reduction, or more to do with less resistance to air flow?
Yes! :lol:
MASSIVE TYPE IV
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Post by MASSIVE TYPE IV »

Both, BUT the airflow on Len's bench wasn't drastiically changed.

We did it because we wanted lightweight, high revving parts that we could use in a super duper street engine and also employ in full race engines.

This is the FIRST affordable 7mm arrangement in TIV history. To this point a set oc custom valves was 450+ bucks, now we can sell you the whole light weight assembly for that or less!
turboteener
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Post by turboteener »

What kind of BSFC are you seeing with this motor? What kind of EGT are you seeing?
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dstar
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Post by dstar »

MASSIVE TYPE IV wrote:True..
I think with a better cam the engine would like even less timing! Maybe as little as 20 degrees!
Jake, do you think the *old* ANNIHILATOR cam that I bought would
like a set of these new Hybrid heads?

Could I still keep the 10.7 CR ratio with these heads?? Maybe higher?
:twisted:

I still want 200hp, I just don't think that *I* can build the engine
that makes it..... it takes a LOT of experience to coax that much HP
out of a 2.3L, four banger, push rodded. OHV engine...
:oops:

Don
mharney
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Post by mharney »

OMG.. did I detect humility?
Guest

Post by Guest »

mharney wrote:OMG.. did I detect humility?
Rare, but THERE!
:lol:

Don
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speedy57tub
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Post by speedy57tub »

Jake,
I would of had loved to have you in my technical staff when I was working in aerospace on some of those :?: projects that don't exist! :wink: After reading your exciting post, now I have to go out and smoke a cigarette (and I do not smoke!) :!: LOL :lol:
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