Update,
Mileage, 60412
Idle jet 45
Main jet 170
Emulsion tube, 75z lowest 2 holes soldered shut.
power jet 47.5
float .032 washer
No choke plate
Boost 12.334
I had a few days to think everything over and decided to do a little test. Found a idle jet marked g45 and decided to see if I could get any leaner afr readings at low cruise rpms.
I found that I had to turn the volume screw out almost 2 full turns in order to get it rich enough to idle without popping. when I tested mid range throttle I found that the AFR would run form 15 to 1 to 12.5 to 1 in cruise. I got a bit of tip in leaness and it would go 18.5 to 1 lean at tip in after a fairly hard run.
Power seemed to be no different and it ran pretty nice except for the lean off throttle area, Specifically when letting off to go around a corner then when accelerating it would falter to 18.5 to 1 for just a bit.
I seemed to have a bit of float trouble too because I noticed after heavy throttle I would get a really rich condition like the float bowl was flooding.
I decided to pull the carb again and do some internal changes.
1. Pulled the top off and replaced the newer float valve with an older one thinking the new one was a POS.
2. Took out the 0.22 washer and installed a 0.33 washer to get the float level down just a bit to keep the fuel form overflowing after heavy boost. Also pulled out the Mexican plastic float and installed the Solex gray float.
3. Pulled the Emulsion tube out again and unsoldered all the holes, cleaned it up and then resoldered the two bottom holes. I figured that I had too many holes soldered shut and that was causing some of the richness at mid range rpm.
I had studied a bit more on emulsion tube theory and came up with the idea that I was causing the rich condition by having the upper holes soldered shut. All I should need is the lowest holes shut since they would be exposed at high rpm which is where I am lean. The upper holes would be exposed at a mid rpm setting which at the time was running too rich.
I took it out for a test even though it was a little wet out.
I have to say that when I hit second gear on boost, it becomes quite a hand full to keep straight!!!!
It was shaking its tail all over the place!!!
It seemed that it has never pulled that hard in second, it really squats down and just takes off like a rocket.. I have no time to look anywhere except the road.....Third gear has very little lag anymore and the afr is running about 14.5. It is still too lean under third gear full boost but I think tomorrow I will be able to fix that if my wire gauge drills show up.
I think I can get the fuel if I drill out the power jet a couple thousandths of a millimeter. Stock is 0.475 mm and I am going to drill it around a 0.50 mm to try first. The power jet is supposed to work at the 4000 rpm to 5000rpm area.
We will see tomorrow.........stay tuned.
Clonebug